Today we started to build a lift that will carry the ball to the launcher. Its a metal lift similar to nicks group that will move the ball to the launcher using tank tread. Also we added wheels to the motors of the launcher that will carry the ball to the wheels that launch the ball. The only problem is attaching this to the robot.
Friday, December 4, 2015
Thursday, December 3, 2015
enemy has spotted us
We scouted the opponents robot performance but saw us and start to shoo us away. Meanwhile our robot performance has been doing so well that it can shoot from the 20 points zone which allows us to shot 5 balls to get a 100 the only problem is the transfer the ball to shotter.
Wednesday, December 2, 2015
Stress
Today are group is stressing because of the fact that we need to be done by next week. we fixed the gearing issue so now we have a medium gear connected to a large gear so now when we tested the gear with the motor even though its a little slower than before it requires less torque to move the gears. Now we have to attach the launcher to the robot and test it with a wiffle ball.
Tuesday, December 1, 2015
Design Flaw
Monday, November 30, 2015
The Mount
We are mounting the shooter on the robot. Knowing that we have only 8 days until the competition we are hoping to beat all other teams. Solidworks has been on hold because our main focus is to finish up the robot.
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